Palau
2012-09-03 03:54:00 UTC
the bike mileage now is 3869km..age is around 13months. bike is fully stock and still under warranty.
[UPDATE]
ask my KTM dealer to use his KTM magic box to diagnose the electronic problem..got one trouble code which if i'm not mistaken is "Rollover input signal too high". not that i know what it means though..even the dealer is scratching his head. he did the ECU reset and now the bike seems ok. the idle even when the problem doesnt kick in is around 1.6k RPM..last time around it was 1.9K..i wont want to jinx the bike by saying the problem is fix yet..still plenty of testing need to be done
[UPDATE]
Cleaning and blowing the moisture out of the BGC "Big Grey Connector" does the trick. the idle is no longer surging and it even felt much smoother now. that could be caused by the ECU reset or Liqui Moly Injector Cleaner...aparently moisture in BGC is known to cause all sort of intermittent weird electronic problem..
[UPDATE 17/07/2013]
Problem is reappearing. foook cleaned and dry and grease the hell out of that BGC multiple time but still same issue. connected a voltage tester on the battery terminal during idle it read 12.43V on engine idle it read 14.04V..seems ok to me. any more possible cause here guys?
Lowrance
2012-09-03 04:12:00 UTC
Palau
2012-09-03 04:30:00 UTC
Post missing.
AGRO!
2012-09-03 06:31:00 UTC
You have to Take the R/H tank fairing panel off and you should be able to see it.
You will have to lift tank so you will need to remove both fairing panels and move radiator overflow bottle out of the way to make the job easier.
Unplug connector and spray isopropyl alcohol on the connectors let it dry and put a nice amount of dielectric grease on the connectors.
What happens is the BGC gets moisture in it and causes havoc with the electronics the dielectric grease stops the problem recurring.
You can use WD40 but i like isoproply alcohol the best.
Palau
2012-09-03 07:31:00 UTC
Post missing.
Palau
2012-09-03 12:54:00 UTC
Lowrance
2012-09-03 16:06:00 UTC
Post missing.
jambox
2012-09-03 18:02:00 UTC
Post missing.
Lowrance
2012-09-03 18:57:00 UTC
Post missing.
Palau
2012-09-04 11:11:00 UTC
Davo-Singapore
2012-09-04 13:19:00 UTC
Palau
2012-09-05 00:09:00 UTC
Post missing.
Davo-Singapore
2012-09-05 02:28:00 UTC
Post missing.
Palau
2012-09-06 07:13:00 UTC
Lowrance
2012-09-06 14:58:00 UTC
DribbleDuke
2012-09-06 15:24:00 UTC
Doing my BGC and local clean-up. I have been plagued by the dash delimna. Clocks are now back to zero miles again. The dash mimics start up cycle while riding and does this mimic in a sporadic timing. Sometimes cycling after three minutes, sometimes cycling before it even finishes a complete cycle.
This may be deeper Than Doug dare do.
As a famous Los Alamitos man said," If you cant fix it with a hammer, it must be an electrical problem."
Ill add if you cant spray solution the problem away, itt must be a mechanics problem.
Crossed fingers.
Sea Foam.
No. 47
2012-09-06 20:58:00 UTC
DribbleDuke
2012-09-06 22:17:00 UTC
Post missing.
MonkeyDuke
2013-07-17 03:59:00 UTC
I wanted to add a word of warning to those using cleaners on the MALE connector:
Be careful of that little orange gasket. It's made of soft rubber and anything like acetone or strong electrical parts cleaner will cause it to shrink and warp. This makes it a real pain in the arse when it's time to put the male and female connectors back together. (I don't care how much lube you use!)
cdlabate
2013-07-17 04:00:00 UTC
Palau
2013-07-17 08:00:00 UTC
ktmguy
2013-07-17 10:21:00 UTC
Post missing.